February 5th, 2018
Today we worked on just trying to get a finished and working robot. We assembled the second carriage, and the plates were also milled and attached. Rohan was milling the right angle brackets that interface with the chain, and Arusha tapped them with the tiny 4-40 tap. She broke one however; good thing we have extras! I think both the battery mounts were completed which is good. One issue was that the inner carriage has about 1/16 of play, which is a pretty big issue. We tried shortening the gab with some plastic taped to the elevator, but I think we will need to mill new plates to adapt and fix the issue.